Thinking Production System To Increase Productivity In Assembly Line

The aim of this study is to evaluate the process of assembling a piston for a door closer manufactured by Dormakaba, a company that specializes in access control and security solution. Lean production is one of the initiatives that are applied by many manufacturers to obtain the competitive advantag...

पूर्ण विवरण

ग्रंथसूची विवरण
मुख्य लेखक: Mohd Rizal, Haziq Rifaie
स्वरूप: थीसिस
भाषा:अंग्रेज़ी
अंग्रेज़ी
प्रकाशित: 2019
विषय:
ऑनलाइन पहुंच:http://eprints.utem.edu.my/id/eprint/25492/1/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf
http://eprints.utem.edu.my/id/eprint/25492/2/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf
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author Mohd Rizal, Haziq Rifaie
author_facet Mohd Rizal, Haziq Rifaie
author_sort Mohd Rizal, Haziq Rifaie
description The aim of this study is to evaluate the process of assembling a piston for a door closer manufactured by Dormakaba, a company that specializes in access control and security solution. Lean production is one of the initiatives that are applied by many manufacturers to obtain the competitive advantages in the increasingly competitive global market. Value Stream Mapping (VSM) is one of the key lean tools to identify the opportunities for other lean approaches and for waste elimination in the production system. Since the performance of the process would significantly influence that of individual partners, the implementation of lean thinking should be carried throughout the development of the VSM. This project introduces the VSM used for description, analysis and identification of improvement initiatives internally in the context of a die-casting manufacturing enterprise. It can be seen from the analysis of the “current state” and “future state” VSM that the non-value added activities which are motion and handling waste within the manufacturing plant can be reduced by the launch of lean initiatives internally. This resulted in developing a solution where the improvement has made a significant impact on reducing waste in the process using tools such as 5S, workstation design and poka-yoke. Overall, the implementation done in the assembly process is shown in the future state map which ensued in decreasing the cycle time by 25%. The recommendation plans for future case study to increase the productivity is to conduct a total produc_(i\'c maintenance for the punching machine in the process that is often delayed due to untrained operators and lack of information on the process management.
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spelling oai:eprints.utem.edu.my:254922022-01-06T11:40:36Z http://eprints.utem.edu.my/id/eprint/25492/ Thinking Production System To Increase Productivity In Assembly Line Mohd Rizal, Haziq Rifaie T Technology (General) TS Manufactures The aim of this study is to evaluate the process of assembling a piston for a door closer manufactured by Dormakaba, a company that specializes in access control and security solution. Lean production is one of the initiatives that are applied by many manufacturers to obtain the competitive advantages in the increasingly competitive global market. Value Stream Mapping (VSM) is one of the key lean tools to identify the opportunities for other lean approaches and for waste elimination in the production system. Since the performance of the process would significantly influence that of individual partners, the implementation of lean thinking should be carried throughout the development of the VSM. This project introduces the VSM used for description, analysis and identification of improvement initiatives internally in the context of a die-casting manufacturing enterprise. It can be seen from the analysis of the “current state” and “future state” VSM that the non-value added activities which are motion and handling waste within the manufacturing plant can be reduced by the launch of lean initiatives internally. This resulted in developing a solution where the improvement has made a significant impact on reducing waste in the process using tools such as 5S, workstation design and poka-yoke. Overall, the implementation done in the assembly process is shown in the future state map which ensued in decreasing the cycle time by 25%. The recommendation plans for future case study to increase the productivity is to conduct a total produc_(i\'c maintenance for the punching machine in the process that is often delayed due to untrained operators and lack of information on the process management. 2019 Thesis NonPeerReviewed text en http://eprints.utem.edu.my/id/eprint/25492/1/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf text en http://eprints.utem.edu.my/id/eprint/25492/2/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf Mohd Rizal, Haziq Rifaie (2019) Thinking Production System To Increase Productivity In Assembly Line. Masters thesis, Universiti Teknikal Malaysia Melaka. https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=117962
spellingShingle T Technology (General)
TS Manufactures
Mohd Rizal, Haziq Rifaie
Thinking Production System To Increase Productivity In Assembly Line
title Thinking Production System To Increase Productivity In Assembly Line
title_full Thinking Production System To Increase Productivity In Assembly Line
title_fullStr Thinking Production System To Increase Productivity In Assembly Line
title_full_unstemmed Thinking Production System To Increase Productivity In Assembly Line
title_short Thinking Production System To Increase Productivity In Assembly Line
title_sort thinking production system to increase productivity in assembly line
topic T Technology (General)
TS Manufactures
url http://eprints.utem.edu.my/id/eprint/25492/1/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf
http://eprints.utem.edu.my/id/eprint/25492/2/Thinking%20Production%20System%20To%20Increase%20Productivity%20In%20Assembly%20Line.pdf
url-record http://eprints.utem.edu.my/id/eprint/25492/
https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=117962
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